I did it today morning along with my brother's help when the bike was fully cold. The rattle sound has reduced a lot. The inlet clearance was wrong, almost 0.08mm! I set it correctly.
One thing I would like to mention is your pics make it seem like there is lot of space around the inlet and exhaust port but actually there is very little
. Had a hard time adjusting with forceps and spanner. Another mistake was I assumed I had 9mm ring spanner & I didnt! So managed with open one, maybe thats why I found it a bit difficult.I also managed to damage the crankshaft rotation bolt
so I set it to TDC using kick lever 
Anyways thanks again for taking the time post DIY. Would have had to visit SVC again if not for this.





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