If the coolant is leaking to oil, then adding 300ml of coolant should definitely have increased the oil level right? But that does not look to be the case as well. Oil level is constant and no bubbling, no milky white color.
Will probably poke a camera through spark plug hole to check how the piston head is looking. If it's related to head gasket, the carbon should be blown off by now. Will the thread updated on findings.




. The compression test came out to be same as previous year reading, no changes in that. But the carbon deposit blown off from the piston head can be clearly seen in the pictures. Even though I use the throttle body cleaner from air filter opening to clean the valves and throttle plates, that might not been responsible for such clean piston head.

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